Meister Kraft
Veteran Member
2001 jetta automatic
DLC 520
GT1749VB
Stock map sensor
Egr delete
Straight pipe exhaust
Stock intercooler
Malone eco tune
Forced economy mode with transmission - 00011 coded in
Recent engine rebuild, stock compression just upgraded rings and bearings
Fault code p0234 for overboosting
No vacuum leaks
Vacuum is pulling 30+ inhg
Set actuator to start moving around 3inhg
Hits stop screw around 24inhg
The turbo was a used unit that worked, I drove the guys car for a few days years ago with no issues. He upgraded shortly after and sold old turbo to me. It sat in my storage bin until needed. I adjusted the actuator because they were all out of spec. First road test with this turbo shows boost building quick under medium load, say 60%+ according to my scan guage. 1st, 2nd, are all ok and I won’t over boost.
Returned to my shop and feed vacuum manually with mityvac and watched the rod and actuator for skipping, found none, left vacuum applied for a lunchbreak and came back to no drop.
2nd road test No change but a few notes
This is the important part:
Problem occurred after GT1749VB was installed
GT1749VB was missing stop screw and the rod length was tamperd with
1st gear all ok
2nd gear all ok
3rd gear TCC unlocked is ok but very close 18psi
3rd gear TCC locked rolling on the throttle I over boost to 23+ and limp mode
4th gear TCC locked is the same as 3rd locked
The delima:
If everything was stock I assume the turbo is faulty or N75 controller, so I put a new n75 in anyway because it’s cheap. Same issue persists. Did I miss something on my inspection, did I misadjust the actuator on the turbo for a GT1749VB, is it my tune?
I need to understand this.
DLC 520
GT1749VB
Stock map sensor
Egr delete
Straight pipe exhaust
Stock intercooler
Malone eco tune
Forced economy mode with transmission - 00011 coded in
Recent engine rebuild, stock compression just upgraded rings and bearings
Fault code p0234 for overboosting
No vacuum leaks
Vacuum is pulling 30+ inhg
Set actuator to start moving around 3inhg
Hits stop screw around 24inhg
The turbo was a used unit that worked, I drove the guys car for a few days years ago with no issues. He upgraded shortly after and sold old turbo to me. It sat in my storage bin until needed. I adjusted the actuator because they were all out of spec. First road test with this turbo shows boost building quick under medium load, say 60%+ according to my scan guage. 1st, 2nd, are all ok and I won’t over boost.
Returned to my shop and feed vacuum manually with mityvac and watched the rod and actuator for skipping, found none, left vacuum applied for a lunchbreak and came back to no drop.
2nd road test No change but a few notes
This is the important part:
Problem occurred after GT1749VB was installed
GT1749VB was missing stop screw and the rod length was tamperd with
1st gear all ok
2nd gear all ok
3rd gear TCC unlocked is ok but very close 18psi
3rd gear TCC locked rolling on the throttle I over boost to 23+ and limp mode
4th gear TCC locked is the same as 3rd locked
The delima:
If everything was stock I assume the turbo is faulty or N75 controller, so I put a new n75 in anyway because it’s cheap. Same issue persists. Did I miss something on my inspection, did I misadjust the actuator on the turbo for a GT1749VB, is it my tune?
I need to understand this.
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